Pilot: Capt. Charles E. Yeager
Time: 14 Minutes
9th Powered Flight
1. After normal pilot entry and the subsequent climb,
the X-1 was dropped from the B-29 at 20,000' and at
250 MPH IAS. This was slower than desired.
2. Immediately after drop, all four cylinders were
turned on in rapid sequence, their operation stabilizing
at the chamber and line pressures reported in the last
flight. The ensuing climb was made at .85-.88 Mach,
and, as usual, it was necessary to change the stabilizer
setting to 2 degrees nose down from its pre-drop setting
of 1 degree nose down. Two cylinders were turned off
between 35,000' and 40,000', but speed had increased to
.92 Mach, as the airplane was leveled off at 42,000'.
Incidentally, during the slight push-over at this
altitude, the lox line pressure dropped perhaps 40 psi
and the resultant rich mixture caused the chamber
pressures to decrease slightly. The effect was only
momentary, occurring at .6 G's, and all pressures
returned to normal at 1 G.
3. In anticipation of the decrease in elevator
effectiveness at speeds above .93 Mach, longitudinal
control by means of the stabilizer was tried during the
climb at .83, .88, and .92 Mach. The stabilizer was
moved in increments of 1/4 - 1/3 degree and proved to
be very effective; also, no change in effectiveness was
noticed at the different speeds.
4. At 42,000' in approximately level flight, a third
cylinder was turned on. Acceleration was rapid and
speed increased to .92 Mach. The needle of the
machmeter fluctuated at this reading momentarily,
then passed off the scale. Assuming that the off-scale
reading remained linear, it is estimated that 1.05
Mach was attained at this time. Approximately 30%
of fuel and lox remained when this speed was reached
and the motor was turned off.
5. While the usual light buffet and instability
characteristics were encountered in the .88-90 Mach
range and elevator effectiveness was very greatly
decreased at .94 Mach, stability about all three axes
was good as speed increased and elevator effectiveness
was regained above .97 Mach. As speed decreased after
turning off the motor, the various phenomena occurred
in reverse sequence at the usual speeds, and in
addition, a slight longitudinal porpoising was noticed
from .98-.96 Mach which (was) controllable by the
elevators alone. Incidentally, the stabilizer setting
was not changed from its 2 degrees nose down position
after trial at .92 Mach.
6. After jettisoning the remaining fuel and lox a 1 G
stall was performed at 45,000'. The flight was
concluded by the subsequent glide and a normal landing
on the lake bed.
CHARLES E. YEAGER
Capt., Air Corps